Wednesday 25 April 2018

Golf gti edition 30 mpg update 30.8mpg 392 miles

Definitely appears 2mpg better after pcv replacement and rear pads replaced

Golf gti edition 30 rear brake pad expired , disconnect seat chime

Started to make grinding noise from rear.  Thought it was a stone in caliper, but on inspection could see the outer pad was down to the backing! Short term I have fitted some mintex rear pads for £16 off eBay.
Caliper was very stiff ends rubber boot damaged so will need caliper refurb or replacement.

Also disconnected the seat sensor as the alarm kept going off at random times during my commute!

Golf gti edition 30 mpg 27.4 mpg 322 miles

Wednesday 4 April 2018

Golf GTI Edition 30 : PCV replacement



Started to get a frequent CEL for P0441 Evaporative Emission System Incorrect Purge Flow.
Cleared the code several times (using a generic obdII reader + phone + obd doctor free)
I was ignoring it (as its not harmful) until....

Drove the 20 mile commute into manchester, parked up and the car had a low idle and was 'hunting'
The boost gauge also showed the vaccum had dropped at idle (from 22in Hg to 16 inHg)!
The revs would also rise up to 2k by themselves then drop (with no throttle pedal)
Pulling dipstick = no change in idle, so it was time to dig out the PCV valve I had ordered from ebay a while back for this very eventuality!

2007 Mk5 Edition 30


As at 2018 the current is 

2.0T FSI PCV Valve  06F-129-101-R bought from ebay £43

Old Versions 06F-129-101-N, 06F-129-101-L, 06F-129-101-K (my old version), 06F-129-101-F, 06F-129-101-C

Revision K for revision R.
114,000 miles
Never been replaced so this was the version from the factory.

Easy change on the drive in the dark
  • Engine Cover off
  • disconnect 2 vaccum lines
  • undo 4 bolts and replace (i kept the old pcv gasket)
Note : I did not replace any other components i.e. the rear check valve

While replacing, I did try blowing/sucking the old and new valves.
Interestingly the old valve appeared to seal ok (in fact even better than the new one!) but when fitted it solved the problem.

vacuum level reverted back to 22 inHg at idle, now smoother.

In theory the MPG should also increase
I never noticed any drop in boost levels during this time

A great advert for having a boost gauge 

heres a pic of the OLD part number , vaccuum levels before(broken)/after(fixed)