The current steed
5 years ago
Automotive
Fiat Coupe 20VT (to 2004)
Mini Cooper S (to 2006)
Honda CBR600RR (2005 to 2006)
BMW M3 E46 (2006 to 2007)
Ford Kuga 2.0TDCI 4wd 163 (2016)
BMW X5 X40d E70 (June 2016 to Nov 2017)
VW Golf GTI Edition 30 (Nov 2007 to June 2018)
Mercedes Benz A180 Auto (W176) (Nov 2017 to Aug 2020)
VW Golf GTI Edition 35 (June 2018 on)
VW Tiguan Mk2 2.0 TDI 150 DSG RLine (Aug 2020 on)
BMW S1000R SPORT (Oct 2021 on)
1 Fault Found:03156 - Sensor for Anti-Theft System (G578) 004 - No Signal/Communication - Intermittent
1 Fault Found:
03156 - Sensor for Anti-Theft System (G578)
004 - No Signal/Communication - Intermittent
Freeze Frame:
Fault Status: 00100100
Fault Priority: 4
Fault Frequency: 1
Reset counter: 155
Mileage: 34479 km
Time Indication: 0
Date: 2012.11.17
Time: 22:10:30
1 Fault Found:
01044 - Control Module Incorrectly Coded
000 - - - Intermittent
Freeze Frame:
Fault Status: 00100000
Fault Priority: 1
Fault Frequency: 1
Reset counter: 255
Mileage: 35267 km
Time Indication: 0
Date: 2012.11.26
Time: 17:06:39
01-Engine -- Status: OK 0000
02-Auto Trans -- Status: OK 0000
03-ABS Brakes -- Status: OK 0000
04-Steering Angle -- Status: OK 0000
08-Auto HVAC -- Status: OK 0000
09-Cent. Elect. -- Status: OK 0000
10-Park/Steer Assist -- Status: OK 0000
15-Airbags -- Status: OK 0000
16-Steering wheel -- Status: OK 0000
17-Instruments -- Status: OK 0000
19-CAN Gateway -- Status: OK 0000
25-Immobilizer -- Status: OK 0000
2E-Media Player 3 -- Status: OK 0000
42-Door Elect, Driver -- Status: OK 0000
44-Steering Assist -- Status: OK 0000
46-Central Conv. -- Status: OK 0000
52-Door Elect, Pass. -- Status: OK 0000
55-Headlight Range -- Status: OK 0000
56-Radio -- Status: OK 0000
62-Door, Rear Left -- Status: OK 0000
72-Door, Rear Right -- Status: OK 0000
77-Telephone -- Status: OK 0000
Volkswagen Mk.6 Golf GTi Edition 35: CDLG EA113 engine bay
Introduction The Volkswagen Mk.6 Golf GTi Edition 35 was powered by a 2.0-litre turbocharged petrol engine (code: CDLG) that was a member of Volkswagen's EA113 engine family. Compared to the 2.0 TFSI engine in the Volkswagen Mk.5 Golf GTi (engine codes: AXX, BWA, BPY and CAWB), changes for the Mk.6 Golf GTi Edition 30's CDLG engine included: •A reinforced cylinder block at the main-bearing pedestals and main-bearing caps;•A new high-flow cylinder head made from aluminium-silicon alloy for high temperature resistance;•Long-duration camshafts and revised exhaust camshaft timing;•Uprated piston (wrist) pins, piston rings and connecting rods; •Annular valve seats;•A larger BorgWarner K04 turbocharger which provided peak boost pressure of 1.2 bar (up from 0.9 bar);•A larger intercooler and radiator cores;•A lower compression ratio of 9.8:1 (compared to 10.5:1); •A redesigned fuel pump and high-pressure injectors;•Four oxygen sensors;•A relocated diverter valve; and,•An upgraded positive crankcase ventilation (PCV) system.
While the CDLG engine of the Golf GTi Edition 35 produced peak outputs of 173 kW at 5500-6300 rpm and 300 Nm at 2400-5200 rpm, the closely related CDLF engine of the Volkswagen Mk.6 Golf R produced peak outputs of 199 kW at 6000rpm and 350Nm at 2500-5000 rpm.
Volkswagen CDLG EA113 engine
ModelEngineTrans.Peak powerPeak torque
Volkswagen Mk.6 Golf GTi Edition 35 2.0-litre CDLG turbo petrol I4 6sp man.,6sp DSG 173kW at 5500-6300rpm 300Nm at 2400-5200rpm BlockThe CDLG engine had a grey cast iron (CG25) block with 82.5 mm bores and a 92.8 mm stroke for a capacity of 1984 cc. Within the cylinders, the contact surfaces were honed by liquid blasting. Furthermore, the CDLG engine had a die-forged steel crankshaft which operated on five main bearings.
To offset second degree inertial forces, the CDLG engine had two chain driven counter-rotating balance shafts.
Crankcase breather systemThe CDLG engine had a crankcase breather system whereby blow-by gases from the crankcase were passed via the primary oil separator in the oil filter module to the cylinder head cover. When this occurred, the blow-by gases were mixed with those from the cylinder head and passed through a labyrinth where further oil separation occurred.
Cylinder headThe CDLG engine had a cast aluminium alloy cylinder head with double overhead camshafts. While the intake camshaft was driven by a roller chain, the exhaust camshaft was belt-driven and had an elliptical toothed belt pulley on the crankshaft to reduce rotational vibrations on the camshaft and pulling forces on the toothed belt.
The CDLG engine had four valves per cylinder that were actuated by roller finger cam followers with hydraulic valve clearance compensation. For heat dissipation, the exhaust valve stems were filled with sodium.
BBorgWarner K04 turbochargerThe CDLG had a single water-cooled turbocharger that was integrated with the exhaust manifold into a single unit. For the CDLG engine, the BorgWarner K04 turbocharger provided peak boost pressure of 1.2 bar (17.4 psi).
The speed of the turbine, and hence charge pressure, was controlled by a charge pressure control solenoid valve and vacuum unit, with the latter actuating the wastegate valve via a linkage. When opened, the wastegate valve created a channel for exhaust gases to bypass the turbine.
To prevent the turbocharger from braking too heavily in overrun and between gear changes, an electric air recirculation valve was used. Ordinarily, pressure would accumulate in the compressor housing during overrun due to the prevailing charge pressure – this pressure build-up would cause the compressor wheel to brake heavily, leading to a reduction in the prevailing charge pressure (turbo drop). To prevent this from happening, the air recirculation valve was opened by an electric servo motor, creating a bypass channel for compressed air to flow from the compressor wheel back to the suction side of the compressor circuit, thereby keeping the turbine at a constant speed. When the throttle valve was opened, the turbocharger air recirculation valve would close and charge pressure was restored.
Fuel Stratified Injection (FSI)The CDLG engine had Volkswagen's 'Fuel Stratified Injection' or 'FSI' which directed fuel directly into the combustion chamber (as opposed to port injection which injected fuel upstream of the chamber) at a pressure of up to 115 bar. The high-pressure fuel pump was driven by a four-fold cam on the exhaust camshaft.
Fuel was only injected in the piston’s compression phase (rather than the conventional induction phase) and was directed into the intake air stream as it moved towards the spark plug. The CDLG engine had two injection modes:•Dual injection for cold starts: a special mode for rapid heating of the catalytic converter, the primary injection occurred on the intake stroke at approximately 300 degrees before top dead centre (TDC) of ignition and the fuel distributed itself homogeneously. The second injection occurred at approximately 60 degrees before TDC in the compression phase. The richer mixture formed around the spark plug such that timing could be retarded and, since the exhaust valves were open during combustion, the hotter exhaust gases contributed to faster warm-up of the catalytic converter (around 30-40 seconds from start-up); and,•Homogeneous injection: injection occurred in the area of the spark plugs with a stoichiometric air:fuel mixture (14.7:1)
Since the engine operated in homogeneous mode during normal running, tumble flaps were used to improve mixture formation. At low loads and engine speeds from 1000-5000rpm, the tumble flaps were closed to:•Improve idle quality after cold starts;•To increase the tumble effect and provide smoother running; and,•To prevent engine jolts.At other engine loads and speed ranges, the tumble flaps were open for free air flow and maximum performance.
IgnitionThe CDLG engine had four single spark ignition coils and cylinder-selective anti-knock control that was controlled by the Bosch Motronic MED 9.1 engine management system. Furthermore, the CDLG engine had a compression ratio of 9.8:1. Article by Ian Lithgow
Note: If you data sample rate is low, expecially if you have no Turbo Mode option with the Micro Can cable, return to the home screen, click Options and change BLK INT to 25 and CHAR INT to 0.so thats what I did, for info the
Blk Int affects the protocol timing. The current default value is 55. To get the highest sample rate possible in the Measuring Blocks screen, set this to 25. Note, however, that this may cause unreliable communications with some controllers. Char lnt 2K / Char Int also affects the protocol timing. This is called Char Int 2K and the default value is 6 when used with a HEX-NET or HEX-V2. This is called Char Int and the default value is 1 when used with a legacy interface. To get the highest sample rate possible in the Measuring Blocks screen, set this to 0. Note, however, that this may cause unreliable communications with some controllers.